I recently took into inventory a 1975 Briggs 3 HP Model 80202. Before I even tried running it or disassembling it for a rebuild I first do a compression test and (now) a cylinder leak down test. Compression was at 100PSI and the leak down test was within specs and acceptable. I then take off the head and inspect the bore. I noticed that there was a LOT of carbon buildup on top of the piston, on the underside of the cylinder head and on top of the deck around the valves. After cleaning all the carbon off I installed a new head gasket and put it back together and rechecked the compression and cylinder leak down. The compression was now at (only) 85PSI,


Michael